So, Miffy is back up and running
It has been an expensive month or so to say the least. After getting the head off I noticed that there were hairline cracks between the glow plugs, injector ports and the exhaust valve. After 220k miles, a blown head gasket and a skim it is a tired head. So I made the decision to purchase a new AMC head from Turners. Expensive, but so far it is all working perfectly.
What was interesting was where silicone sealer had made its way to... That stuff is just plain evil. Useful but evil... This is the build-up around the hydraulic lash adjuster. Just how much is gumming up the adjusters?! who knows... Replace those then...
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The heat damage to the glow plug wiring was unexpected, but with a good quality of amalgamating tape the connections are working well. Will keep an eye on them.
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The injectors looked superb after 220k miles, nothing external, no build up or bits missing.
Bagged. Tagged. Clean. Ready.
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The block looked in good condition. A little surface rust in the coolant ports, nothing major. Once clean there was almost no wear waft or warp across the top of the block. a few minor scores in the third cylinder bore, but nothing major. I know that I will have to do a bottom end rebuild in the future, but not for a while and hopefully once I have a roof for Miffy to sit under whilst I take the engine apart...
So the AMC head... Superb quality and the upgrades to the injector port walls are immense. I built up the head with inlet and exhaust manifolds and then lifted it in to place. Goodness that was an awkward lift... A crane next time I think
Then through the head bolt tightening sequence which is harder than it reads, but thanks to the additional turning assistance of the Tirfor handle over the top of a breaker bar all the bolts were torqued down to specs. The entire time muttering, please don't shear, please don't shear...
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Fit the rest of the ancillaries, fill the coolant, oil, filters, etc etc... Purge the fuel system... First turn of the key
Gaud love ya Miffy... Can't keep the big girl down...
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The new head has now done around 700 miles or so, mixture of driving and she pulls like a freight train. Smoke is normal, if anything better than before and oddly the exhaust does not smell as much as it used to at idle. Maybe those cracks where something... The MPG is bob on 26-28 over a couple of tanks. No leaks (touch wood). So far so good...